(slightly edited to shorten message; boldface type added for emphasis)
March 3, 2004
Mr. Roy A. Anderson
President and Chief Nuclear Officer
PSEG Nuclear LLC - N09
P. O. Box 236
Hancocks Bridge, NJ 08038
SUBJECT: ANNUAL ASSESSMENT LETTER - SALEM NUCLEAR GENERATING STATION
(REPORT 05000272/2004001 AND 05000311/2004001)
Dear Mr. Anderson:
On February 4, 2004, the NRC staff completed its end-of-cycle plant performance
assessment of
Salem Units 1 and 2. The review involved the participation of all technical
divisions in evaluating
performance for the calendar year 2003 assessment cycle. The process included a
review of
performance indicators (PIs) for the most recent quarter and inspection results
from 2003. The
purpose of this letter is to inform you of our assessment of your safety
performance and our plans
for future inspections at your facility so that you will have an opportunity to
prepare for these
inspections and to inform us of any planned inspections that may conflict with
your plant activities.
Overall, Salem Units 1 and 2 operated in a manner that preserved public health
and safety and
fully met all cornerstone objectives. Plant performance for the most recent
quarter at Salem Unit 1
was within the Regulatory Response Column of the NRC’s Action Matrix, based on
an inspection
finding in the Mitigating System Cornerstone being classified as having low
to moderate
significance (White) and all PIs being Green. The White inspection finding
involved inadequate
corrective actions to prevent the recurrence of emergency diesel generator (EDG)
turbocharger
failures, which resulted in the 1C EDG turbocharger failure in September 2002.
In a follow up
inspection report dated January 30, 2004, the staff kept this White finding open
until additional
inspections confirm that final corrective actions have been implemented.
Plant performance for the most recent quarter at Salem Unit 2 was within the
Licensee Response
Column of the NRC’s Action Matrix, based on all inspection findings being
classified as having
very low safety significance (Green) and all PIs being Green.
As discussed in the annual assessment letter dated March 3, 2003, and the
mid-cycle assessment
letter dated August 27, 2003, the staff identified a substantive cross-cutting
issue in the area of
problem identification and resolution (PI&R). The cross-cutting issue
involved instances of
ineffective, untimely problem evaluations and corrective actions. In the most
recent
2 Mr. Roy Anderson
annual assessment, we concluded that this substantive cross-cutting issue should
remain open,
based on the numerous inspection findings which indicate that weaknesses
continue in this area.
The weaknesses impacted equipment reliability and involved deficient
determinations of root
causes. For example, inspection findings included the deferred fuse uprating of
control drive
mechanisms, which resulted in dropping of control rods and a manual Unit 2
reactor trip; an
inadequate operability evaluation of offsite power supply breakers following a
Unit 1 partial loss of
offsite power; insufficient evaluation of an air leak on an EDG starting air
compressor; and
incomplete preventive maintenance and inadequate corrective actions for the
control air system.
We request that you discuss this matter at our upcoming annual assessment
meeting.
In a January 28, 2004 letter, we provided interim results of an ongoing NRC
special review of the
work environment at Salem and Hope Creek. The letter outlined areas of NRC
concerns,
particularly as they relate to the handling of emergent equipment issues and
associated
operational decision-making. The letter also requested a written response to
provide a plan for an
in-depth PSEG assessment of the work environment. We have received your response
and are
reviewing your plans. We expect to discuss this matter with you at the
management meeting
specified in our January 28 letter (tentatively planned for mid-March).
The enclosed inspection plan details the inspections scheduled through September
30, 2005.
The inspection plan is provided to minimize the resource impact on your staff,
and to allow for
scheduling conflicts and personnel availability to be resolved in advance of
inspector arrival
onsite. In addition to the baseline inspections at Salem through September 2005,
we plan to
perform a supplemental inspection on the open White inspection finding to review
the corrective
actions for the EDG turbocharger failure. The inspection is intended to provide
assurance that the
corrective actions address the root cause of the failure. Routine resident
inspections are not
listed due to their ongoing and continuous nature. The inspections in the last
twelve months of
the inspection plan are tentative and may be revised at the mid-cycle review
meeting.
As you are aware, the NRC has issued several Orders and threat advisories to
enhance security
capabilities and improve guard force readiness since the terrorist attacks on
September 11, 2001.
We have conducted inspections to review your implementation of these
requirements and have
monitored your actions in response to changing threat conditions. For calendar
year 2004, we
plan to continue inspections of order implementation combined with newly
developed portions of
the security baseline inspection program.
In accordance with 10 CFR 2.790 of the NRC’s “Rules of Practice,” a copy
of this letter and its
enclosure will be made available electronically for public inspection in the NRC
Public Document
Room or from the Publicly Available Records (PARS) component of NRC's document
system
(ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/readingrm/
adams.html (the Electronic Reading Room).
3 Mr. Roy Anderson
If circumstances arise which cause us to change the inspection plan, we will
contact you to
discuss the change as soon as possible. Please contact Glenn Meyer of my staff
at
(610) 337-5211 with any questions you may have regarding this letter or the
inspection plan.
Sincerely,
/RA/
A. Randolph Blough, Director
Division of Reactor Projects
Docket Nos. 50-272, 50-311
License Nos. DPR-70, DPR-75